Wednesday, November 25, 2015

Montero Automatic Transmission Fluid and Filter Change

To begin with, I am sorry to disappoint the destruction fanatics with this post. As opposed to destroying something recently,I have actually improved an object of significant worth to us. And to be honest, I would prefer to see more of these types of posts.

 
Montero Sport
The err gold..brown..green..Montero Sport. Straight out of the jungle.


I drive a 2009 Mitsubishi Montero Sport. This 7-seater, sport-utility vehicle (SUV) has a 2.5L direct injection diesel engine, and has an automatic transmission. It's quite a reliable vehicle as it is both economical and safe - albeit there are some isolated reports of Sudden Unintended Acceleration (SUA) accidents you can find on news sites which are also tested by some on Youtube. It's mileage is now running at 47,000km and I knew it was already due for a change in its AUTOMATIC TRANSMISSION FLUID (ATF) and ATF FILTER. Most, if not all, of the car enthusiasts would have their cars serviced by authorized dealers. I think this is always the best route. But for me, aside from just trying to save on budget, my curiosity simply just got the better of me. 

So I bought the necessary materials for my "operation" a few days before the weekend. I was able to source the OEM transmission fluid and its filter, a silicone gasket maker, and a funnel to help me pour the fluid into the dipstick tube. I also prepared the hydraulic jack, wrenches, sockets, pliers, and some cleaning materials. 

So I started by lifting the vehicle a couple of inches higher off the ground to create some clearance underneath. I would suggest that you try to lift it up as much as you can, otherwise you would be working your butt off literally, commando style, or like an upside down frog (you know, the ones you run over the highway). I began the more difficult work by removing the front bash plate. There were actually two of them at the bottom, so I took both of them off to expose the transmission coolant hose.

transmission coolant hose
The transmission coolant hose line


I released the clamp with the use of some pliers and disconnected the rubber hose from the metal tube that lead to the radiator. I connected the metal tube to a small hose that lead to my oil basin. I released the Kracken err- the hydraulic jacks to restore the vehicle to its normal angle. I then started the vehicle at the Neutral position, and the old transmission fluid started to drain out of the hose line, which lead to my basin. After draining the fluid and switching the engine off, I transferred the old fluid with the use of a funnel to some empty soda bottles - these were 2-liter bottles - so that I could have an idea of how much fluid would be replaced. I was able to drain out 4 liters of the old transmission fluid. 

I had to lift the vehicle again to be able to commando crawl - yes like the upside down frog - under the vehicle and loosened the transmission drain plug. I placed my catch basin underneath the area of the plug and then lowered the vehicle once again. I also took out the dipstick from the transmission tube to allow the flow of fluid out of the drain.

After draining,  I raised the vehicle to start loosening the bolts so that I could take out the transmission pan. This was a bit more difficult because of the space constraints, the tension on the bolts, and the gasket. I was finally able to remove the bolts - except for one on each of the sides, I just had to make sure that the pan doesn't just fall off completely - and the pan was still too difficult to pull out. It turned out that the gasket was really tough to take off, and the pan was not budging at all. I used a couple of flat head screwdrivers to slowly create some leverage at one corner of the transmission pan. Eventually, after a couple of wedging, I was able to take out the pan and pour the remaining fluid inside of it, into my basin. 

Transmission
The exposed ATF Filter after the pan is removed. Watch out for drippings!
 
Transmission Pan
The pan with the magnets and a little fluid left


The transmission pan contains 3 magnets. I would assume that these magnets attract the metal filings within the fluid to help the filtration process, maintain viscosity, and avoid damaging the transmission gears. I found the magnets to be quite dirty or grimy, with very fine materials attracted to it. I also checked the pan for any large metal filings that could indicate damage within the transmission. The good news was, there weren't any.

So that's how dirty the magnet was. That's also how dirty my fingernails were.

I took out the 3 magnets, bearing in mind it's locations, and easily cleaned each one of them by wiping away the grime. I also cleaned the pan thoroughly, and started working on the silicone gasket around it. It took quite some time to take it all out from the sides of the pan because of how much material was on it. I removed the old ATF filter - it was secured with 2 bolts that I kept - and pulled it out from the transmission. It contained some of the fluid so I had to drain it into the basin as well. 

The discarded ATF Filter. Out with the old-
 
-and in with the new. The new ATF Filter.



I also had to take out and clean the gasket material on the sides of the transmission and wipe away any visible grime with a clean piece of cloth. 

 
Automatic transmission
I really tried to make it as clean as I could


I then installed the new ATF Filter and used the bolts I got from the discarded filter. 


Automatic Transmission Filter
With the new filter installed

At this point I just wished I could afford my own creeper. My back, both of my arms, and my neck were killing me. But since I already got this far, I was determined to soldier on. So now that the pan was clean, I applied the new silicone gasket maker on the sides of the pan. I found varying opinions on how much sealant to place, but I decided to put a continuous bead sized application of it, all over the sides. And when everything was done, I put the pan back on the transmission. Two things I would notice would be: First, since the pan was colored black, perhaps next time, I should use a different colored silicone gasket maker, maybe a pink colored one, or a brown colored sealant. I think a similar colored sealant would be difficult to spot the next time I would try to clean it. The second observation would be that even the bead sized application was seeping out of the sides as I tightened all the bolts in. 

automatic transmission
So now my aching body could not even take a decent photo under the vehicle


So now that the pan was back in its place, I lowered the hydraulic jack and prepared to pour in an initial amount of the new ATF - I think I poured in about 3 liters of the new fluid. I used a funnel to pour in the new ATF through the ATF dipstick tube. I then started the vehicle at the Neutral position and drained the remaining old fluid via the hose that I set-up at the transmission coolant line. I was able to drain another 1.5 liters of the old fluid from it. I "guess-timated" that there was close to 5.5 liters of the old fluid that I drained, therefore, I needed to replace it with the same amount of the new one. Since I had 3 liters already, I just needed to add about 2.5 liters. Prior to adding the remaining amount, I had to reconnect the transmission coolant line, which means I had to reconnect the rubber hose to the metal tube and reattach the clamp on it so it doesn't leak.

Mitsubishi ATF SPIII
The ATF SPIII that I used


Pouring in the final 2.5 liters had to be done in a painstaking manner because I didn't want to overfill the ATF. So I had to pour in a few amount every time and then check the level again with the dipstick. I was also shifting through the gears at certain points - meaning I shifted around P-R-N-D a couple of seconds each gear- all these with the engine running. 

When I was able to achieve the right level, I put everything back in its place. I had to take the vehicle for a test drive to see if there were any problems, and the good news was that there weren't any problems. After I parked the vehicle, I checked for any leaks under the vehicle as well. 

It has been almost a week since I did the change, and so far so good. The transmission seems to be a lot smoother and I haven't encountered any problems with the vehicle. I just hope it stays this way, so I'm keeping my fingers crossed! Next up, the engine oil, but maybe after my sore back recovers from all this "upside down frog"-ing around.

Tuesday, November 17, 2015

Clamp

The CLAMP or C-Clamp is a great tool to hold, lock, or fasten objects together. It is a versatile tool that carpenters can use to hold boards or lumber in order to nail or glue them together. Metalworking can also make use of these tools to hold metal sheets or bars together prior to welding, cutting, drilling, riveting, or grinding. Basically, anything solid that you want to be held stable, can be clamped. 

Clamp
The remains of the clamp because the Force was just too much
 We tried to create a DIY sheet bender to fabricate small changes in our block mould. We tried copying what was shown on the internet, making use of available materials we had, and bought Lotus clamps from the hardware. Our inexperience with the tool led us to purchase the 4" sized clamps. These clamps as you may observe from the picture above are made up of cast iron which is a brittle metal. We tried bending a 5mm sheet of metal at a 45 degree angle, but as we approached about 20 degrees, there was a light snap that sent parts of the clamp flying a short distance. The clamp was undersized, and could not handle the force needed.

We tried using 8" clamps from the same brand to try and bend the sheets again to no avail. It seemed like the clamps were starting to bend a little bit as we were approaching close to 40 degrees and we did not want to risk another rocketman phenomenon with the larger clamps. We were also no longer confident with the materials that the clamp was made up of. There were some clamps in the hardware store that were not made up of cast iron, but the prices of which were not economical to us. Other brands such as Stanley seemed to look rigid enough, but then the prices were double that of the Lotus brands. So we decided to look for an alternative solution that did not cost us too much to bend the sheets of metal we needed for our mould.

We have seen some other DIYs on the internet that made use of larger machine bolts as an alternative to clamps. However, this would require making a hole at the metal base for the bolt to be inserted. But considering that the bolt is made up of stronger steel than a cast iron clamp, this would prove to be the safer solution. The bolts are locked in tight with the nuts, and its threads help in ensuring this. The steel bolt diameter of 1" also gives us peace of mind because breaking this will require a tremendous amount of force.

Despite not being able to push through with its planned use, we still use the remaining 8" clamps for different purposes at work. Mostly, it helps in fastening the boards that we nail to make the hollow block trays. The ease of locking and releasing the boards from the worktable makes the job faster and safer. The next time we use it for other types of jobs though, we just have to remember how much force the clamps are going up against to avoid costly mistakes.

Sunday, November 15, 2015

Hammer

Most HAMMERS, if not all, are disposable. We use them a couple of times, then by some stroke of luck, some part of the hammer goes off. It is quite surprising to know that this tool can easily be discarded and replaced with a new one most of the time since the hammer is an essential tool for carpenters and even masons. Anything that needs to be nailed, demolished, or just hit with blunt force can be done with a hammer. 

 
The hammer of Thor


In our particular experience, we often use a claw hammer for its versatility to drive and remove nails. We often use hammers to repair wooden pallets, and make wooden trays for our block production. However, the head always starts to get a bit loose, then eventually goes off the handle. Even the higher priced hammers like the Stanley brand would still break. The hammer pictured above was a Sentry hammer. After using it for about a week, the head eventually came off, so in order to save a bit of money, we wrapped its joint between the head and the handle with a piece of cloth that was dipped with industrial epoxy, and let it cure for about a day. Just like a carbon fiber wrap! So far, the fix worked and the head seemed to be more stable now than when we first bought it. 
The Mjolnir with an apron on its neck

Wednesday, November 11, 2015

Screwdriver

Sometimes we don't understand when enough is enough. How much force should we exert when we try to unscrew something? I guess in most cases our answer would be "as much as we possibly can". And in most cases, the tools are the ones that give up. Case in point, our Ju Tai SCREWDRIVER broke its slotted tip after we tried opening an electric motor. 
The victim of the "force"
Even the toothfairy can't give refunds for these
 
The screwdriver even says that it is made out of "Chrome Vanadium", so maybe it's supposed to be tough. It was such a waste of a perfectly good screwdriver, it had a magnetized tip that was handy for picking up the screws or small bits of metal, and it also had a soft rubber handle that provided a better grip for tough twists. Too bad indeed.

Leave it to "Ze Germans" to get it done


But at least we were able to open the motor with the help of another screwdriver, this time, a Kadris screwdriver, which we don't even remember where or when we purchased.It only says "Hardened Chrome" on the rod and had the brand name and Germany on the hard plastic handle. At least it got the job done.

Best to use some penetrating oil like WD-40 that could help loosen the screws a bit before using "the force" on it. Saves your tools, and doesn't damage or deform your screws!

Magnetic Contactor

Our machine is run with control switches with MAGNETIC CONTACTORS or magnetic starters (CHINT brand). These are necessary to run the electric motors of our block machine. A current goes through the contactor, and its electromagnet pulls back its moving contacts and brings it together with the fixed contacts to rapidly send a large amount of current to the electric motors.

These contactors are designed to be robust especially with our machine where some of the motors run at least 100 cycles each day. So, imagine a light switch that you flick a hundred times a day, but in this case it doesn't just switch the light on, but the switch itself is involved in a complex mechanism. 



The Sassin Contactor replacement that also burned up


One of our contactors seemed to be replaced much earlier than the others. It seemed odd that the electrical guy who first installed this used a "smaller capacity" contactor, when in fact the motor it operates is one of the larger ones. The damaged contactor was immediately replaced at first with a similar capacity contactor from a different brand - Sassin (though both Sassin and Chint are made in China), but after a week, the same thing happened. We decided to get a larger capacity of the same Sassin brand, and so far its been months since any problems arose.We are however tempted to try our some German brands, but costs of these are prohibitive.

The larger capacity contactor
But obviously, the best advice we can give is to consult your electrical engineers to determine the correct ratings of your electrical components. This would avoid further damage, and potential harm to the workers.

Tuesday, November 10, 2015

Pinion Shaft

After discovering that the helical gear in our gearbox was damaged, we also found the PINION SHAFT to be severely damaged as well. This had to match with the helical gear's teeth so the machine shop had to fabricate a new 2" diameter pinion shaft for us. 
The damaged pinion gear
 Total downtime to have both gears fabricated was about three weeks because of the steel hardening process that was involved. This affected production schedules and cost us a lot of money, not including the cost of fabrication. We decided to increase frequency of periodic maintenance shutdowns to avoid major problems like these in the future.

Helical Gear

A few weeks ago, we did something to our Hollow block mould to improve the shape and size of our resulting blocks. This resulted to a heavier mould - my guess would be about 40kgs added from the existing 150 kgs. Unfortunately, the machine's mechanical gear box seemed to experience difficulty in lifting the the entire mould box together with concrete materials (approx 100kgs) inside. It was able to function for about a week, but afterwards, it seemed frequently to stop about half way through lifting. 

Gearbox
Gearbox minus the gears and shafting
We were too lazy to take the machine apart and expose the gearbox. So we first thought about the 3hp induction motor that was driving the gearbox to be the culprit. Hence, we checked its A.C. Contactor and replaced it with a new one. Nope, that didn't work. We finally decided it was the gearbox. 
 
Gear with Shafting
The damaged gear with its shafting (plus someone not wearing safety shoes)

 We took it apart and voila, the 10 inch helical gear was missing a number of its teeth on two different areas of the circumference. We foolishly thought there would be a replacement gear readily available in your leading hardware stores. Surprise surprise, it had to be machined. In the end, we had to have the entire gear fabricated using hardened steel. The old one was made out of casted steel.

Helical Gear
Damaged gear with missing teeth. If it doesn't have teeth, then it sure won't bite!
The machine shop told us to always check for the acceptable loads to avoid future problems with the gearbox. Also check alignments, not to over-tighten the belts, ensure proper lubrication of both gears and bearings. Well, we failed miserably on step number one alone. Lesson learned. But that single gear wasn't the only problem. 

To be continued..